My air cooled crank
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Nope, it had stock crank and mains, but had carrillo's and JE's. Got the head off tonite, still not exactly sure what caused the failure. #3 piston is stuck in the cylinder at an angle. I got the crank rotated a bit and got the rod out through the side of the block.
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Grr;240954 wrote:
Gonna need a dingle ball hone and 1 new rod and piston, should be good to go!
Looks like you need to go with the billet rods and a larger pin like matt has for next year, that thing should take a 300shot, 150s are for sissysand a bucket of bondo to fix the hole in the block. then your set!
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DelSlow;241028 wrote:
Vtec must have engaged pretty hard.Yup! Thats it! Case closed........ :icon_geek:
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Wow messy one. When did this happen Dave?
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Sweet-WRX-Lovin;241213 wrote:
Wow messy one. When did this happen Dave?The pass after the 8.04 at the last TM Street Legal.
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I'm sorry but LMFAO at 8.87 @ 118 and you needed another winter project anyway right?
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